I finally was able to get back into this great forum. Although it may take a while,as I have about three projects ahead of it, the two Much will be re built and flying. Yeh!--the pressure was on and I really should have hung it up til next year and used the time to properly test and trim the plane.There were three factors that led to the crash and two of them were my fault. The leadouts were just a bit too far forward and the week engine was mounted on the inboard nacelle. I was too jacked up about flying officials this year.
Thank you all for the nice comments as they are surely appreciated.
Bart